router

Problems and solutions

I was having some issues with the lead nut carriers splitting when I bolted them down, so I decided to try cutting these parts from the Trex composite decking. The piece I bought was 1.125in thick, 5.5 in wide, and 8ft long for about $18, I cut it with the same 2 flute end mill I have been using with MDF, and I think they came out well.

Given that the part is now wider and contains a mix of saw dust and plastic, I am pretty sure I will not have the splitting issues.

Trex Parts
Trex Parts

One more step…

I got a little time last Wednesday to work on the machine, so I went ahead and built the table top.  It consists of of a 59.5 inch x 24 inch sheet of 3/4 MDF that has (3) 56.5 inch sections of  .75 Inch EMT conduit attached to the bottom for support.   The conduit is attached by (5) .25 inch x 2 inch screws spaced 13 inches from each other that are counter sunk into the table.  The table is attached to the machine using 6 more of the .25 inch by 2 inch screws that attach to 3 cross dowels in each end of the machine.  Nothing too exciting, but its another step down.

Completed table attached to machine
Completed table attached to machine

A sagging concern…

Jordan Sipsip left a comment which among other things asked if I had noticed any sagging of the rails.  I really had not noticed any issues with the rails flexing under the weight of the gantry, but I decided to do a quick test.  I stacked a number of pieces of wood under the center of the longest rail so that they were almost/barely touching the rail.

Flex Test Starting Position
Flex Test Starting Position

I then moved the gantry to the edge of the stack and attempted to remove the top most piece of wood…  it slid out without any binding at all.  While not very scientific, I think this demonstrates the minimal flexing issues I have observed up to this point, and bodes well for the future.

The build goes on…

Well thanks to the vacation, holidays, and the drop in temperature it has been about two months since I have done any appreciable work on the machine, but I had a productive day yesterday and thought I would post an update.

I have completed all of the lead nuts and carriers, bearing blocks, and added a support to the bottom of the Y axis to firm things up.

ISO View 1

New build started

I have being playing around with designing a new router since about the start of July 2009, I had actually started cutting out parts for Joe’s 2006, but so many of the larger parts were too big for my current router and were going to have to be joined, that I stopped cutting and starting thinking about designing the kit that I would have liked to have when I was first searching.  So after after 6 weeks of prototyping parts, I started cutting out all of the parts for what I hope will be an easy router that can be sold as a kit that would allow someone to get up and running quickly without having to spend a few months building a router with hand/power tools.

I have already veered of my original intent a bit, but if this thing actually works well, I have plans on simplifying  a few areas to make it so I can ship a fairly small kit with the end user supplying a number of standard size pieces of lumber, well see what happens with that.

The router is designed to have a 24″ x 48″ cutting area, the machine dimensions are ~36″ x 60″, all the rails are designed to use black gas pipe and roller bearings, as in all things I work on, containing costs is one of the prime objectives.

This is about where I stand at the moment, I just added the z rails right after this picture.  I have a fair way left to go, the 1/2″ acme lead screws are here, the 4 270 oz motors are here, I am going to attempt to make my own lead nuts and couplings, so much work still lies ahead, I will do my best to post updates as the major pieces come together.

The build so far...
The build so far…
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